Register To Comment
Page 3 of 18 FirstFirst 1234513 ... LastLast
Results 21 to 30 of 172

Thread: Team Thrifty /Fifty Build Diary for Bitza

  1. #21
    Ohh and I'm sure if we where just to wash all the mud off the robot (it's mostly made from an old lawnmower) it would drop some weight........

  2. #22

  3. #23
    Really?

  4. #24

  5. #25
    Hhhhmmmm, this had crossed my mind.

    Guess I need to think up something!

  6. #26
    We are almost done (although we have been saying that to ourselves for a while now!).

    The robot it now within the weight limit, all of those bugs mentioned earlier have been fixed and some fine tuning has been done.

    Ears and front uprights have been added, so not much more we can add to the robot now.

    We do have one nasty bug though, where we seem to be about 75% down on power and can't figure out why. Unless we get this sorted before Birmingham then we will be useless in the arena.

  7. #27

  8. #28
    The EXACT setup was, two 7.2v NiMH bats in series (with the link separating them), connected in parallel to 2 15amp Electronize ESC (each with a 25amp fuse), these then connected directly to the drill motors. The Tx was the Radio Link T4UE and the old 6 channel Rx. Nothing else was in the chain, no light, mixers, external failsafes, nothing.

    The power drop happened after some modifications, which are as follows;
    Now the Rx has been changed to the newer 7ch option (since the old one broke). The fuses were increased to 35amp, I added a power light and I neatened up the wiring, which included shortening some sections and lengthening others to make the whole thing sit better.

    Other changes included, adding bike tread to the wheels to improve traction and ground clearance, (since the old wheels where smooth and barely stuck out from the chassis) straightened the chassis so that both wheels have equal clearance on both sides of the bot, re-made the motor mounts (old ones came loose) and tweak the wheel mounts so they spin free and smooth with no fouling. I then conditioned the batteries and ran the bot to find the current issue.

    One thing that has changed is the new motor mounts grasp the drill motors on the piece of plastic above where the grub screws go in, before the shaft exits the gearbox. They grasp it with downwards and side force. Could this be inhibiting the motor?

    We also found that the robot no longer drove straight, one side had a lot more power than the other, whereas before it drove straight and true.

    We don't use a mixer, just old fashion tank steer on the 2nd and 3rd channels of the controller.

    My initial thought was that the motors had just accumulated crap over time inside the motor casing, but we had taped the air vents at the very start to stop this.

    Any ideas?

  9. #29

  10. #30
    Quote Originally Posted by PJ-27
    My initial thought was that the motors had just accumulated crap over time inside the motor casing, but we had taped the air vents at the very start to stop this.

    Any ideas?
    Could the motor have over-heated?

Register To Comment

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •