got some images of the robot so far.
will post a video of the new axe when i upload it.
also their is a problem with the chain, for some reason the sprocket isnt straight, this is causing the chain to jam and be looser when the axe is back.
the chain has only came of once, but i think thats because its hitting the motor mount and knocking the chain off. the drive sprocket also came off so had to refix it.
also the motor doesnt seem to be able to lift enough to flip my robot if its flipped. so il eventually buy a new motor and axe (think the handles causing the problem). il also be able to get a motor with the sprocket on it, i think that may be causing a few problems.
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