im not quitting but im thinking i might have to redesign the entire thing as i still want 6 wheel drive but i fear that the interferance caused by 6 motors is enough to send something mental might remove 2 and see how it behaves
You got a V tail mixer in there?
Retry the set up with the rx and the esc outside the bot.
yup just gave that a try its working fine with everything outside the bot...guess im gona need a long teather
Remember milly ann bug?
i remember the milly ann bug i loved that thing and harry i honestly haven't a clue according to the screen everything is set to off if my understanding of the instructions is right
The milly ann bug comment was meant as a fun one, hinting that you could add a 'cart' behind your bot to house the electronics.
I personally never experienced interference originating from my motors while using a 2.4ghz tx/rx.
I actually believed it to be an impossibility.
i did too thats why i wasent originally worried but after that test run i think its safe to say that a redesign is on the cards might look at a belt drive and only run 2 motors
ok folks first the good news after a plea for help about mixing its all been sorted..ish needs tweaking but thank you shakey
after getting that into what i thought was a drivable state i decided to film exactly what is wrong with my bot in the hope that someone can watching it and point out the obvious thing that i am missing somewhere:
couple of this firstly you will need to skip forward as dumbass me forgot to get it in the camera and secondly the wheel escaping was my own ineptitude and not the technologies
please feel free to shout out any observations and yes the wiring is a mess and i haven't made a rear or top for it yet
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