After a true first test drive being completely useless, with the Elctronize test speedos on variable pwm, meaning their low end control was rubbish, I was actually pretty disheartened. It didn't appear to have a chance of being controllable.

Today I tweaked the speedos some and, despite their clunky nature, managed to get it driving to a point where a video was worth it:



Extra points for the box of electronics taped on top!

Will be getting a Scorpion XL kindly put forward by Harry for Deeside, and I still have hopes to get a gyro in there. Add the centre of gravity being improved, as the electronics gradually relocate actually inside the body, and the overkill nature of it might become remotely usable.