Progress is being made, albeit slowly! Many bulkheads cut, holes tapped, and a lot of the robots structure is in place.

The weapon testing showed that the current design has a very underpowered weapon, as the robot won't self right with the current setup. So taking inspiration from other Featherweight axes I'll reengineer this to use a hefty brushed scooter motor and chain/sprocket setup.

I would like to give brushless a try as I think that would give it extra kick, but using big brushless setups is beyond my working knowledge just yet. I'll be off now to do some more research